FJWALLY wrote:Thanks Craig - and Dave - my motor is juts about done and should get gearbox back next week and new clutch is on the list of must do's while it's apart.
Hey Rob
Make sure the flywheel is ground too otherwise it's only 2/3 done ...
vmx-mxr wrote:The old ute is looking good Craig, and the vid was well done - especially "beer o'clock"
Can I gather the aftermarket one you used is the later 8.6" diameter set
Cheers
Dave Mac
Thanks Dave, yep 220mm. I posted the link above which has the pictures of it in my FB post.
Early knock off today. Too bloody hot in the shed. Finished off changing the plywood floor in the back. Bastard of a job.......you cant weld wood lol.
Anyway buggered off to the river to cool down.
parisian62 wrote:Well done Craig! Good times. I remember when we got the wagon on the road there was a ticking noise and we thought was coming from the clutch / gearbox. Luckily it turned out to be the fan was flexing.
Thanks Stuart. I'll keep that in mind too. Still lots to get through but well on the way to making Renmark.
That ute looks great. Good to see youve got it going. as for the noise, can you access the offending area through the hidey hole in the bell housing or are your floor mats too good to pull up to get the cover off. If you can get that cover off you may be able to do something TRICKY in there with a die grinder. Am I on to something or have I forgotten something basic?
Tony.
Plenty of options I'll keep in mind. Tony I don't have any floor mat in it as yet. Just doing the water leak tests here and there before I commit to putting it in when I get it. Access it through the cover plate wont be any good as I know that area wont be where I want to grind. Getting the die grinder in will be like putting toothpaste back in the tube.
Wally I've taken note of Dave's post re machining the flywheel.
I think for the moment I'll run it for a bit and see what happens (head in the sand option!).
Wheel alignment done today. Had to improvise a bit as I haven't got a track rod to do the toe in. Steers well now and holds a straight line with no hands. Steering wheel nice and straight too.
Went up in main jet to 55 to accommodate the cam and to get over a slight hesitation. Pulling well off the line.
Had a great find too. Busted out some NOS Trico wiper blades and fitted them up. Cleaned up the windscreen and noticed some numbers showing up on the glass with the residual water. Hard to explain but.......the numbers are 52653S and circled 311. First one matches the chassis number....311 I have no idea about. Anyway looks to be the original windscreen.........maybe.
Thanks Greg, yep its not that hard but I've learnt one thing with these old busses regarding caster. Trying to get more than 1 degree change in caster is nearly impossible with what adjustment is available. Unless you index the wishbones in a staggered fashion (between top and bottom) its just about impossible to get the required caster spec for a ute. As it is I can only get sedan spec.
Today I've had a crack at doing an epoxy repair on the steering wheel for RWC. Stay tuned on that one. Also started to wire in the trailer plug (lovely Australian made Utilux 5 Pin original with towbar). Dog at least approves of the tray!
Wally I did +1 degree camber +1 1/2 degree caster & 1/16" toe in. Ute specs for caster are 0 to +1 caster but I couldn't get it down that far as I ran out of adjustment (both sides). Either way its within caster spec for sedan and steers well. I'll have to get back to later and work it out. I had similar issue with my FB sedan but not as bad. Might have to go through the service bulletins.
Today I finished off the trailer wiring. Ended up using and old loom and th3 4 way connecters and bullets. Took some fiddly solder work but come up well. Looks factory.........but no one will see it anyway............dunno why I bothered lol.