My bro rocked up to help, so we ran a compression test. I couldn’t believe my eyes. Numbers I saw (psi) were:
130 - 125 - 123 - 130 - 132 - 130
So I turned my attention to the ‘old’ Grey, wrapped up under my workbench since 2013, from a car that was parked in 1999. Filled the cylinders with WD40 and oil and gingerly turned it over by hand until it stopped and the push rod on no.3 exhaust valve kicked off at a big angle: the push rod is very bent, and the valve is stuck in it’s guide.

Soaked the valve stems also and waited then turned again by hand. With a loud crack, the valve went down but never came back up. Dang.
With the motor at least now spinning free, I hooked up a battery and jumped the starter solenoid for a compression test on the garage floor:
78 - 105 - 0 - 55 - 80- 120
So. My original impressions were wrong. Just because I can spin Leroy’s motor over so easily from the fan belt, doesn’t mean it has low compression... I’ll now get that one up on a stand and dismantle only as far as I need too. Probably leave pistons in their bores and just lift the crank to do rear main seal. Suss out bearing condition and evidence of oversizing etc.




Meanwhile, I also have the driver’s door off and stripped for a look at “just one 20c piece sized rust bubble” as all the ads on Unique Cars say. Surprise surprise, I could almost put my fist through the hole I cut it back too.
At least the door liner provided some evidence that the windscreen seals were replaced when the hood lining was done



hehe got yas

More updates soon.
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